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#1 |
![]() Join Date: Apr 2012
Location: Pineville, Louisiana
Posts: 57
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Need some help guys...
Finally got my car back together after refinishing the engine and doing a couple other things. First start up: starts up great but idling at 2100 rpm, take my foot off clutch and it climbs to 2500 rpm then after about 4 secs climbs up to 2800ish. I shut off car at that point, engine ran for no more than 30 secs. We check throttle cables, they seem to be fine. Belt had slipped off so re-positioned it and started engine a 2nd time. Same exact symptoms, starts at around 2100 rpm then climbs up to right under 3000 rpm, I shut engine off again at that point. List of everything we did to car while apart: Secondary system removed Charcoal system removed New FIC SS injectors Chip tone (Pete) Any suggestions would be greatly appreciated ![]() |
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#2 |
![]() Join Date: Dec 2003
Location: Chicagoland,IL
Posts: 2,667
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Sounds like you have a big vacuum leak.
By the way how did you plug the holes when you took off the secondaries. I had a freeze plug fell off on one of the secondary holes. Did you plug the vacuum port under the plenum that went to the EVAP solonoid? When you ported the TB are the throttle blades closed? Just in case i doubt it but try stock chip. Pete
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'91 #1635 PoloGreen 350 LT5 11.09 @ 129.27 11.04 @ 128.86 474RWHP 400RWTQ http://www.youtube.com/watch?v=SFNFOhGGlR4 http://www.youtube.com/watch?v=ZlRIOMwaDYY https://sites.google.com/site/peteszr1garage Last edited by Pete; 10-26-2012 at 02:24 AM. |
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#3 |
![]() Join Date: Jan 2009
Location: Portland Oregon metro area (Washington side)
Posts: 3,193
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It maybe tiime for a data logger. Need to find out if it's getting
into closed loop. The fact that it's going backward over time is curious. (going higher rather than lower) See what happens when you unplug the IAC. Also pull the bellows and watch all three plates for movement as the idle increases. Getting any codes set?
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Scott ![]() Vett owner since 1979._It's about the car and the people Last edited by scottfab; 10-26-2012 at 10:37 AM. |
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#4 |
![]() Join Date: May 2007
Location: Westminster, Maryland
Posts: 3,684
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I agree with Pete. The symptoms you describe sound like a vacuum leak. I have had it happen to me. Did you put o-rings on all 16 injectors at the injector housing. Some year LT5's require an oring that is in the housing.
Try removing the bellows at the throttle body air horn and block the air flow to the throttle with a STIFF board, a binder cover works well. With the air horn blocked, the engine should stall. If the engine doesn't stall, you have a vacuum leak. Good luck Jim |
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#5 |
Join Date: May 2007
Location: Chicagoland, IL
Posts: 9,686
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Since you ported TB, have you done the Min Air adjustment?
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#6 | ||||
![]() Join Date: Jan 2007
Location: Pineville, LA
Posts: 584
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![]() Quote:
Pete, I couldn't find a vacuum leak this was my first thought I will pull the plenum and check. The Dorman plugs were used to cap the secondaries and I don't see them coming out but will also look at that. The port under has been capped. The TB was done by the PO all I did was refinish it and reinstall. Everything operates smoothly without any binding. I don't have a stock chip but I will pull the one off of my Z and see how that works or if it changes anything. Quote:
Scott, No codes are being thrown. I will try the IAC tonight and see what that gets me. Quote:
Yes, new O rings in the IH's (where needed) and on the injectors form FIC (where needed) had the O rings already installed so it is all new. Thank you for the tip I will give it a shot. Quote:
We did not port the TB just refinished it when Tommy Morrison had the car the TB was done this was in the late 90's. Thanks for all the advice guys we will see where this takes us. Daniel |
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#7 |
![]() Join Date: Apr 2012
Location: Pineville, Louisiana
Posts: 57
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Pulled plenum, freeze plugs look good and everything seems to be connected or capped off from secondary system...
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#8 | |
![]() Join Date: Jan 2009
Location: Portland Oregon metro area (Washington side)
Posts: 3,193
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Another ZR-1 on the road is the goal.
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Scott ![]() Vett owner since 1979._It's about the car and the people |
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#9 |
![]() ![]() Join Date: Dec 2003
Location: Grand Island NE
Posts: 1,512
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I don't know if it is the same problem as what I had, but I had my throttle body enlarged to 63mm and I assume new throttle blades were installed to fit the new sized bores.
Then later I had the throttle body powdercoated. Afterwards I experienced high idle. Mine would start off with normal idle until I drove it, but then after driving it would always idle high until I shut it off and restarted it. I was told that the baking of the throttle body in the powdercoating process that the bores might be now odd shaped from the blades. Made sense to me that heating of aluminum could make these openings change shape. I sent my throttle body to Marc Haibeck for rebuild and all is good now. Did you do the test Jim mentioned or the adjustment XfireZ51 suggested. If you don't have a vacuum leak, you might be experiencing what I did.
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Dennis Fierstein 90 ZR-1 #2562 Atomic-Z ZR-1 Net Registry Chairman of the Board ZR-1 Net Registry Treasurer |
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#10 | |
![]() Join Date: Jan 2007
Location: Pineville, LA
Posts: 584
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That makes sense but it seems to work just fine. The Z hasn't run long enough to heat up yet. I have not had a chance to try any of the tests I am still at work for a few more hours at the moment ![]() ![]() Daniel |
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