09-02-2017 | #11 |
Join Date: May 2007
Location: Chicagoland, IL
Posts: 9,704
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Re: So I had a bit of blowby...
I have datalogged my car enough to know that I don't have detonation. The top end timing doesn't induce any detonation. In researching this, I came across
this video by Hastings in piston ring failure. https://youtu.be/3GbXxf435N4 One of the causes listed is "lugging" the motor. During some datalogging sessions, I have "lugged" the motor intentionally. Sometimes 6th gear at 900rpm as a way of gathering readings on VE cells not typically used in normal driving. So I'll be avoiding that in the future. Why just #7?
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[SIGPIC][/SIGPIC]Former Membership Chairman Former ZR-1 Registry - BOD 1972 Corvette 4speed base Coupe SOLD long time ago 1984 Corvette Z-51/4+3 SOLD 1992 Corvette ZR-1 Aqua/Gray #474 SOLD 1992 Corvette ZR-1 Black Rose/Cognac #458 2014 Honda VFR Interceptor DX |
09-03-2017 | #12 |
Join Date: Mar 2007
Location: Crystal Lake, IL
Posts: 7,193
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Re: So I had a bit of blowby...
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LGAFF 90 #966-150K miles-sold 92 #234-sold 1987 Callaway TT #17 1991 ZR-1 #1359 |
09-03-2017 | #13 |
Join Date: May 2007
Location: Chicagoland, IL
Posts: 9,704
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Re: So I had a bit of blowby...
Thanks Lee. Very interesting. I don't typically floor it in 6th and low rpm, but a a prolonged deliberate lugging of the motor could be the culprit.
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[SIGPIC][/SIGPIC]Former Membership Chairman Former ZR-1 Registry - BOD 1972 Corvette 4speed base Coupe SOLD long time ago 1984 Corvette Z-51/4+3 SOLD 1992 Corvette ZR-1 Aqua/Gray #474 SOLD 1992 Corvette ZR-1 Black Rose/Cognac #458 2014 Honda VFR Interceptor DX |
09-03-2017 | #14 |
Join Date: Nov 2011
Location: Dunbarton NH
Posts: 7,469
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Re: So I had a bit of blowby...
Well, I'll be avoiding lugging the motor a lot more. Thanks Dom.
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09-04-2017 | #15 |
Join Date: May 2007
Location: Chicagoland, IL
Posts: 9,704
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Re: So I had a bit of blowby...
So a bit of an update. A couple of "while you're theres".
Replacing clutch disc and rod bearings. In the course of diagnosing the the cracked compression ring, Pete removed the rod end. He found the top portion of the bearing to be worn to the copper while the bottom end appeared to be fine. No issues w the rod journals. He surmises that this may have happened at engine initial startup. The motor came out of the 92 Aqua ZR and was a service replacement to the original motor. Pete suspects that since the service motors may have sat for some time, the top portion of the rod bearing had drained of oil, and startup of the motor without proper pre-oiling may have caused the wear. Also, I am replacing the stock LT1 clutch disc I have been using. I have suspected that possibly the clutch could be slipping at top end after having done a series of mods that should have resulted in an increase of trap speed. Instead the trap has remained relatively flat and really isn't indicative of the power the motor is making. The disc we have removed shows signs of wear and is pretty thin. Replacing it w Centerforce sprung hub which has more "meat" to it. As you can see in the attached pics, the CF disc utilizes more of the area in the center to increase friction surface and several others like the way it works with their Fidanza FW.
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[SIGPIC][/SIGPIC]Former Membership Chairman Former ZR-1 Registry - BOD 1972 Corvette 4speed base Coupe SOLD long time ago 1984 Corvette Z-51/4+3 SOLD 1992 Corvette ZR-1 Aqua/Gray #474 SOLD 1992 Corvette ZR-1 Black Rose/Cognac #458 2014 Honda VFR Interceptor DX Last edited by XfireZ51; 03-08-2024 at 03:10 PM. |
09-04-2017 | #16 |
Join Date: Nov 2013
Location: Wilkes-Barre, PA
Posts: 148
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Re: So I had a bit of blowby...
I ran a Centerforce clutch in the GS before swapping to a auto. Drove like stock, pulled 1.5x 60's with it.
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1994 ZR-1 #198, sold [img]https://live.staticflickr.com/65535/48400173802_2a6f122cfb_n.jpg[/IMG] [COLOR=RoyalBlue]96 GrandSport#857[/COLOR],[COLOR=Red]Red Gut[/COLOR] 397 LT4, AFR heads,3:90 gears, DRM longtubes, Sepanek 700R4, Yank 3600, bla-bla... Best ET w/396 & 6-speed 11.02 @126.57 w/1.60 60' Best ET w/396 & 700r4 10.82 @124.87 w/1.48 60' 2003 DarkShadowGray Ford Lightning 460rwhp/550rwtq 12.11 @112.18 w/1.71 60' |
09-04-2017 | #17 | |
Join Date: May 2007
Location: Peoria, AZ
Posts: 9,155
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Re: So I had a bit of blowby...
Quote:
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GOLDCYLON - 91 ZR-1 #2014 GOLDCYLON - 90 ZR-1 #2794, 4L60e (Formerly Schrade's) GOLDCYLON - 11 CTS-V Arizona State Director 91 WHITE/BLACK #2014. 380 P&P&PCed,Ported Heads, Jeal Long tubes, Corsa Exhaust/FIKSE FM-5s /LED TLs, LED Headlights, Front Wilwood 6 piston narrowlite calipers and rear Wilwood caliper street shop mod,CNCed Coolant Pipes,TPI Cvr,Filter cover,Stainless Bolts, DRM/DOM PROM /ZFDOC mod build #102,DRLs,BMAD with stainless Debris Screen,Coplan Air Blaster, Pioneer APP Radio 4,Brey-Krause HB,Sub Bar,Fire extinguisher seat mount,DRM Coilovers,LEDs everywhere,Compass mirror (orange),V1 DIC hidden display, Homelink sun visor, Carbon Fiber top x3 and APSIS Carbon Fiber interior, APSIS CF Steering Wheel/NAPA Leather, Banski trailing arms, Guldstrand front suspension,urethane bushings from Prothane (total suspension) ZFDoc drive shaft safety loop, raptor shift light (orange),AO engineering louver front plate, Console seat cushion, 96CE seats with black custom Sheepskins, ss billet catch can,Viper remote entry/alarm,Cragar Rear Louvers,LED side louver lights, Dewitts Radiator with SPAL fans and a Woods 160 T-Stat 90 RED/BLACK #2794. 4L60e Automatic Stage V by RPM Transmission, TCI Dedicated TCM, OBX Stainless Headers, Corsa Exhaust, SAN Secondaries and Haibeck PROM, Exotic Muscle Coil overs, LED Interior Lights, LED Tail Lights, LED Headlights, 94 Sport seats with black custom Sheepskins , Cragar rear louvers, GS Front calipers, Banski Trailing arms, APSIS Carbon Fiber steering wheel, Front and Rear Baer Eradispeeds, DRLs, Guldstrand front suspension,urethane bushings from Prothane (total suspension), Dewitt's Raditor with Dual SPAL fans and a Haibeck 170 T-Stat 11 RED/GREY CTS-V |
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09-04-2017 | #18 |
Join Date: May 2007
Location: Chicagoland, IL
Posts: 9,704
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Re: So I had a bit of blowby...
The one I am replacing is a stock OEM LT1 clutch disc. So will be using the Centerforce. With 345s in back, I probably could use the clamping force.
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[SIGPIC][/SIGPIC]Former Membership Chairman Former ZR-1 Registry - BOD 1972 Corvette 4speed base Coupe SOLD long time ago 1984 Corvette Z-51/4+3 SOLD 1992 Corvette ZR-1 Aqua/Gray #474 SOLD 1992 Corvette ZR-1 Black Rose/Cognac #458 2014 Honda VFR Interceptor DX |
09-08-2017 | #19 |
Join Date: May 2007
Location: Chicagoland, IL
Posts: 9,704
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Re: So I had a bit of blowby...
Below is a view of the top compression ring from #7. Also, motor is starting to go back together. Before Pete started, we discussed cc'ing the heads just to make sure we had all uniform chambers. Pete verified that they were uniform
40cc chambers. We did this on the suggestion of Marc H. Wanted to check if there was some other explanation for compression being overall somewhat lower on the driver's v passenger side banks. However, the FSM states compression should not vary greater than 15% from low to high cylinders. We're ok there (210 v 245). And FSM states that high end of adequate compression is 200psi. So we are over that by a significant number.
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[SIGPIC][/SIGPIC]Former Membership Chairman Former ZR-1 Registry - BOD 1972 Corvette 4speed base Coupe SOLD long time ago 1984 Corvette Z-51/4+3 SOLD 1992 Corvette ZR-1 Aqua/Gray #474 SOLD 1992 Corvette ZR-1 Black Rose/Cognac #458 2014 Honda VFR Interceptor DX Last edited by XfireZ51; 03-08-2024 at 03:10 PM. |
09-08-2017 | #20 | |
Join Date: Apr 2007
Location: Lake Bluff, IL
Posts: 2,090
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Re: So I had a bit of blowby...
Quote:
Did the little pieces of the ring stay in the groove or did you have to go fishing in the oil for them?--Bob
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2016 Long Beach Red Z06 #10281 "POPS Z" 1995 Polo Green #409 "WARP TEN"--Haibeck 350/510 package, 4.10s, Hurst, Stock Exhaust with QTP Cutouts --Sold but still running strong 1993 Quasar Blue #161 "HIL KING" --Sold but still running strong, now with more than 120,000 miles 1967 Marlboro Maroon/Saddle Corvette Coupe 300 hp/4-spd --Sold a long time ago ZR-1 Net Registry Founding Member #95 NCM Lifetime Member Favorite Quote--Attributed to Mickey Thompson: "Too Much Horsepower is Almost Enough" |
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