05-03-2017 | #51 | |
Join Date: Mar 2014
Location: Warrington PA
Posts: 1,914
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Re: Further idle diagnosis....
Quote:
Now, as mentioned before this was after the first plenum pull. So apparently something was disturbed causing this issue. As mentioned in my other thread, going to go over everything, install new plenum gaskets. And also learned that the primary blade is not to be completely closed and that no "dag" was used on that blade. Also brought to my attention that the lines I mentioned in the other thread concerning the connector are EVAP lines. So maybe there was a loose connection in the one that came out real easy. I don't know, but hopefully will get all of this resolved.
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Tom 1994 ZR-1 #009 "captured test fleet car" 1974 LS4 454 Vert 1974 L-82 355 Vert. 1982 L83 CFI...now a retired "dd"....Sold WAZOO Member |
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