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#1 |
![]() Join Date: Sep 2011
Location: montgomery tx
Posts: 65
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I have pulled this plenum three frickin times to fix vacuum leaks and starter the third time crank no-start was a dreaded bent pin now it starts and runs great however saw white steam out of exhaust and immediately shut it down. no water in oil and plugs are clean. i had some antifreeze get in a secondary forgot to drain the third time shop vac it out and before starting pulled plugs and blew out cylinders by turning it over. what the hell have i done. it finally was idling at 704 and idc was at 43 not zero and she runs great. please tell me it didn't totally screw up as this was my inheritance and right now i am sick to my frickin stomach.
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#2 |
![]() Join Date: Mar 2007
Location: Crystal Lake, IL
Posts: 7,180
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coolant leak.....did youuse new gaskets? and where did you get them from?
If you got some in the IHs.....does not take much to create a lot of smoke..
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LGAFF 90 #966-150K miles-sold 92 #234-sold 1987 Callaway TT #17 1991 ZR-1 #1359 |
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#3 |
![]() Join Date: Sep 2011
Location: montgomery tx
Posts: 65
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My father owned an Auto parts store and Had several sets of gaskets and before i sold the store I built a stock pile of plugs wires rotors calipers compressor alt. starter etc. there is no water in oil at all and antfrezze system will hold pressure could this be what the residule in Ih and it just needs to run I really dont want to f this up first plenum pull and it has been rough. wish dad were alive i need a little moral support right now.
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#4 |
![]() Join Date: Mar 2007
Location: Crystal Lake, IL
Posts: 7,180
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Its possible, some may have moved into the exhaust and is buring ogg... if they are stock gaskets they should not leak. I am sure you know this, but just in case, there is coolant that runs through the plenum.
Best bet would be to drain some of the coolant out of the drain **** and pull it to inspect and reseal. PITA, but no way to guarantee whats going on without being there.
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LGAFF 90 #966-150K miles-sold 92 #234-sold 1987 Callaway TT #17 1991 ZR-1 #1359 |
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#5 |
![]() Join Date: Sep 2011
Location: montgomery tx
Posts: 65
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should i let it run and see if steam stops she runs so damn good and has no hesitation the idle is perfect no codes found in history fuel pressure is perfect. just pulled all plugs and none are washed hell none were wet. now what should i do turn it over again with no plugs and there ( and inj fuses pulled') and there was nothing to come out of cylinders should i run it for a few or yank this prick again.
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#6 |
![]() Join Date: Sep 2011
Location: montgomery tx
Posts: 65
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do you mind calling me 936 828 1908 so we can chat
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#7 |
![]() Join Date: Sep 2011
Location: montgomery tx
Posts: 65
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DOES ANY ONE ELSE THINK THE SAME I STILL HAVE NOT STARTED IT KIND OF SCARED
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#8 |
![]() Join Date: Sep 2011
Location: montgomery tx
Posts: 65
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oK I HAVE DRAINED RADIATOR AND PULLED PLENUM GASKETS LOOK BRAND NEW DOES NOT SHOW ANY LEAK. I DRAINED ALL THE OIL NO WATER FOUND AT ALL. NEW OIL AND FILTER AND CLEANED UNDER PLENUM YET AGAIN. I REPLACED ALL SOFT RUBBER VACUUM LINES AND USED IDEAL CLAMPS AND ZIP TIES ON SMALL FITTINGS WITH THE MIGHTY VAC HOLDS 50NG STRONG WITH NO LEAK DOWN AFTER 5 MINUTES. REPLACED COILS AND WIRES FOR THE HELL OF IT AND CHECKED SECONDARIES ADJUST AND ALL SEEM CLOSED TIGHT. THE NEW MSD COILS LOOK GREAT. CHANGED ALL PLUGS WITH AC DLECO PLATINUMS AND GAPPED AT .35. REFILLED RADIATOR AFTER FLUSHING IT AND ADDED TO BOTTLES OF WETTER AND NEW ANTIFREEZE. ALSO NOTICED SERP BELT HAD CRACK ON UNDERSIDE SO R&R THE SERP BELT AND THE TENSIONER JUST FOR SAFE KEEPIN. PUT A NEW OPTIMA BATTERY AND CHECKED FUEL PRESSURE 57 OBS HOLD STRONG. ALSO BLEW OUT DRAIN IN INTAKE VALLEY AND USED BLUE LOCTITE ON COIL BRACKET AND THE BRACKET IN THE FRONT SOME OF THOSE BOLTS WERE HAND TIGHT. I THINK I HAVE IT ALL FINISHED, GOING TO TAKE A 1 HOUR COOL DOWN BREAK AND THEN TRY TO START YET AGAIN. GENTLEMAN THE FIFTH TIME BETTER BE THE CHARM. I HAVE DEFINATLY POPPED THE PLENUM CHERRY.
"No bastard ever won a war by dying for his country. He won it by making the other poor dumb bastard die for his country. " ![]() George S. Patton |
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#9 |
![]() Join Date: Sep 2011
Location: montgomery tx
Posts: 65
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ALSO WHY DOES IT SAY L98 UNDER MY NAME IT IS AN LT5 CAN SOME ONE FIX THIS PLEASE
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#10 |
![]() Join Date: Feb 2011
Location: San Marcos CA
Posts: 1,786
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It sounds like you didn't drain the water lever down far enough and just dribble some coolant into the intake ports. If it didn't break it already, you'll be fine. pulling the plugs was good insurance for that.
it will just steam for a couple of minutes. If there was so much as to get into the mufflers (like when a head gasket blows), it could take 15 minutes, but I think you'll be fine. |
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